i've been beating my brain a little trying to figure out a problem with my S6 avant for some time. oh when i bought the car it was stock for starters. the first thing i did was install a boost gauge so i could see what the current boost levels where with the car and i would see 14psi a most and it would bleed down to around 8psi at the top of the RPM. With the current setup listed below and the boost goes above 16psi it seems like the car loses has no power. with the MTM chips i see 19psi at most and when on an average it seems to go to 16psi and bleed down to 10psi at the top of the rev range. when i see boost levels above 16psi is when im crusing and i floor it the car seems to spike up to 19psi and kind of hold there than around 3500 it jumps down to 16psi and starts tapering off to 10psi. the whole time its above 16psi the car feels gutless. i cant think of whats causing this for the life of me, i've ran every option through my head and nothing add's up. well one thing comes to mind when and that the MTM chip has too much timing in the lower RPM range and its making the engine knock which is making it pull timing when it spikes above 16psi. i've driven plenty of cars on the same chip set and they dont seem to act like this at all. all of the other cars didnt have boost gauges so i couldnt see what was going on but they didnt have this slugishness that my car does. anyone have any ideas what it could be? i considered modifying the MTM timing/fuel chip and removing some timing from the map to see it that cures the issue but i feel its not going to.
here's a list of what i've done to it since just for reference.
-custom 3in turbo back exhaust with single muffler and enxternal dump wastegate
-Ebay RS2 turbo manifold
-Custom intake with open element filter
-31x12x3 front mount intercooler with custom piping. piping starts at turbo with stock rubber hose and goes into 2.5in pipe to the intercooler, than from the inercooler to the throttle body is 3in pipe.
-Forge motorsport splitr diverter valve with external vent capped off.
-Custom 1.8T coil pack conversion with NGK BKR7EIX iridium plugs gapped to 24 thousandths.
-ECU has MTM1+ chip set with 034 varimap set to 3bar.
well thats my issue/story, any input on what might be causing this would be great because i know its not running at its full potential.
Here's a few pictures of the engine bay for reference.


